Disaster Averted, though I still have a problem! | <– Date –> <– Thread –> |
From: jim (jimshadow![]() |
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Date: Sun, 9 Nov 2008 07:49:06 -0800 (PST) |
Well, it was bound to happen sooner or later.... Lets back track just a bit. Back in July I parked the GT4 to address a noise that I had tracked to my front bank tensioner bearing. They were last replaced 3yrs ago and I've put about 10-12,000 miles on her in the last 1.5 yrs. (I DRIVE this little GT4!!!) Not wanting to have a belt failure, I decided to do the belts, bearings and give her a valve adjustment. All went well and I got it back together just in time to road test and drive it 1200 miles r/t to Mississippi for the '308's in '08' Event. The car performed like a champ and the noise had all but disappeared, that is until I got down to the Memphis area. At the event I had Rick Lindsay and Ric Rainbolt give a listen. Both agreed that it sounded strange and that it was likely a bearing somewhere. Fast forward home and I'm out with a buddy grabbing coffee and going to see a '63 Vette with '96 internals and 700ish HP. (Keep in mind that i've not driven it since returning from the '308 Event but once). Well, that damn noise was back, but this time getting louder and sounding worse, much worse. Upon pulling into the 'Vette owners driveway I looked under the car and noticed black oil on my alternator and on the frame near the balancer which is not one of my usual leaks. So I limp the car home at 25mph and park it. Today I started taking things apart and found that my front bank lower drive gear was COMING OFF the shaft! I could spin the nut with my fingers. The only thing keeping it on was the belt cover. You can see in the pics where the gear was bumping into the cover and scoring it. The ironic thing is that I was just checking prices this past week on what it would cost to finally do the sodium valves as preventive maintenance, now this! I was convinced that the noise was my water pump bearing and I was going to be torqued that I didn't do a 'while i was in there' and rebuild it when I was doing the valve adjustment/belts. I was all ready to fire the car up today and get out my mechanics stethoscope to figure this out when that nut caught my eye. THANK GOODNESS that the gear did not let loose and throw my belt off!!! I'm grateful for that for sure. I'm confident that I can do the bearing job myself, however, I'm debating just pulling the motor and sending it off to get the head work done as well as the bearings and a couple other things....stay tuned and wish me luck! JIM (PS, my marks all line up, so no jumped belt teeth or anything like that. I could not feel any play in the gear other than the slightest in/out movement from that loose nut.....)
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Disaster Averted, though I still have a problem! jim, November 9 2008
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Re: Disaster Averted, though I still have a problem! rolindsay, November 9 2008
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Re: Disaster Averted, though I still have a problem! jim, November 9 2008
- Re: Disaster Averted, though I still have a problem! Doug and Terri Anderson, November 9 2008
- Re: Disaster Averted, though I still have a problem! rolindsay, November 9 2008
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Re: Disaster Averted, though I still have a problem! jim, November 9 2008
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Re: Disaster Averted, though I still have a problem! rolindsay, November 9 2008
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